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| LDEQ Incident Number Incident Date |
Point Source(s) | Notes | Amount of Release |
| 05-BB005-210 2005-05-11 | K3304 | Cause: Leak on the Hydrodesulphurization (HDS) Unit Off0gas Compressor K-3304 Followup: No Notes: Sweet streams (lower Sulfur content) were routed to the flare to minimize sour gas flaring. Process unit output was adjusted in order to minimize the total amount of waste gas being sent to the flare. | 388.0 pounds |
| 78361 2005-04-19 | K-401 (waste gas compressor number 2) | Cause: Waste gas compressor number 2 (K-401) automatically shut down, automatically diverting waste gas to the flare system. Followup: No Notes: Low-Sulfur content streams were routed to the flare to minimize sour gas flaring. Output was adjusted to minimize total amount of waste being sent to the flare. Same language about doing an investigation to understand the underlying cause and prevent future incidents. | 19.0 pounds |
| 78341 2005-04-17 | K-401 (waste gas compressor number 2) | Cause: Waste gas compressor number 2 (K-401) automatically shut down, automatically diverting waste gas to the flare system. Followup: No Notes: Low-Sulfur content streams were routed to the flare to minimize sour gas flaring. Output was adjusted to minimize total amount of waste being sent to the flare. | 14.0 pounds |
| 78226 2005-04-13 | K-401 (waste gas compressor number 2) | Cause: Waste gas compressor number 2 (K-401) automatically shut down, automatically diverting waste gas to the flare system. Followup: No Notes: Low-Sulfur content streams were routed to the flare to minimize sour gas flaring. Output was adjusted to minimize total amount of waste being sent to the flare. Letter rescinds report of nitric oxide because below reportable quantity. | 42.0 pounds |
| 05-BB005-157 2005-04-06 | K-402 (Refinery waste gas compressor number 3) | Cause: K-402 unexpectedly shut down. Shortly after shutdown, refinery personnel identified the cause of the shutdown as a malfunction of the compressor motor ignition system. Followup: No Notes: The compressor motor was repaired and the compressor restarted, ending the incident. | 651.0 pounds |
| 77936 2005-03-31 | K-400 (Refinery waste gas compressor number 1) | Cause: Refinery waste gas compressor number 1 (K-400) unexpectedly shut down. Refinery waste gas automatically diverted to the flare system. Followup: No Notes: Adjustments made to the fuel/air mixture and K-400 restarted. | 14.0 pounds |
| 77659 2005-03-17 | No information given | Cause: Waste gas compressor number 2 (K-401) automatically shut down due to a high temperature. Followup: No Notes: Letter rescinds verbal report because incident was not reportable. No release to atmosphere. | 42.0 pounds |
| 05-BB005-135 2005-03-13 | C-2307 (Second Stage High-Pressure Separator) level controller; K-2303 (HCU Second Stage Recycle Compressor) | Cause: During maintenance, the Hydrocracker (HCU) Second Stage High-Pressure Separator (C-2307) level controller was inadvertently left in the manual position. Later, HCU Second Stage Recycle Compressor (K-2303) shut down due to high level in C-2307. Shutdown of K-2303 caused automatic depressurization of C-2307 to the refinery flare system. Followup: No Notes: Letter rescinds report of Sulfur Dioxide because below reportable quantity. | 176.0 pounds |
| 05-BB005-128 2005-03-02 | Waste Gas Compressor Number 4 (K-406); Copper tubing connecting C-435 (first stage suction drum) to high-level instrumentation | Cause: Waste gas compressor number 4 (K-406) shut down due to failure of piece of copper tubing connecting C-435 to high-level shutdown instrumentation. When it failed, a false high level reading was recorded, causing automatic safety shutdown system to become engaged. Followup: No Notes: Low-Sulfur content streams were routed to the flare to minimize sour gas flaring. Output was adjusted to minimize amount sent to the flare. C-435 was retubed, K-406 was checked and restarted. | 182.0 pounds |
| 76869 2005-02-11 | No information given | Cause: From the verbal report: Followup: No Notes: | 93.0 pounds |
| 05-BB005-113 2005-02-07 | Unintended over pressurization of the Hydrocracker Light Ends Plant (HCU LEP) Depropanizer surge drum | Cause: Due to the isolation of the sight glass of the hydrocracker light ends plant depropanizer, the automatic level indication equipment was disabled and false reading was transmitted; this condition caused an unintended over pressurization of the HCU LEP Depropanizer surge drum, which was venter to the refinery flare system (No. 2 flare) Followup: No Notes: Refinery personnel evaluated the process operation, identified the source of the problem and made appropriate corrections, ending the incident. | 545.0 pounds |
| 05-BB005-106 2005-02-04 | Electrical breaker G-457; Waste gas compressor number 2 (K-401) | Cause: Electrical breaker for G-457 malfunctioned. Waste gas compressor number 2 (K-401) shut down as a result of the electrical power outage and refinery waste gas was diverted to safety flare system. Followup: No Notes: Low-Sulfur content streams were routed to the flare to minimize sour gas flaring. Output was adjusted to minimize total amount of waste being sent to the flare. Note: the breaker for G-457 had been identified for repair and was supposed to be replaced that week. | 78.0 pounds |
| 05-BB005-100 2005-01-24 | Waste gas compressor shut down and caused an over pressure situation | Cause: From the verbal report: Followup: No Notes: | 46.0 pounds |
| 05-BB005-93 2005-01-22 | K-406 (waste gas compressor number 4) | Cause: Waste gas compressor number 4 (K-406) unexpectedly shut down. Waste gas was automatically diverted to refinery safety flare system. Followup: No Notes: Note: This compound was not included in the body of the letter. It was listed in a chart attached to the letter. | 138.0 pounds |
| 76362 & 76355 2005-01-21 | Hydrocracker Light Ends Plant Butane Splitter Tower & LEP Depropanizer Tower Bottoms Flow Control Valve 50FC060 | Cause: (1) 0600 hrs: Hydrocracker Light Ends Plant (LEP) Butane Splitter Tower began to overpressure because LEP Depropanizer Tower Bottoms Flow Control Valve (50FC060) had failed in the open position, letting propane to exit to the Butane Splitter. (2) 1700 hrs: Butane Splitter again began to overpressure due to the presence of propane. The level indication on the level instrument was detecting a false reading. Followup: No Notes: Letter speaks of two incidents on same day at 0600 hrs and 1700 hrs but attached report shows three incidents: (1) 4:05 a.m. lasting 3h 42m; (2) 3:15 p.m. lasting 41m; (3) 4:30 p.m. lasting 1h 25m. Amounts of compounds are only given in totals for all 3incidents. | 452.7 pounds |
| 76224 2005-01-18 | No information given Number 2 Flare -- Pressure Safety Valve (PSV) on Fuel Drum for Number 10 Boiler | Cause: From the verbal report: Followup: No Notes: | 1,805.0 pounds |
| 05-BB005-67 2005-01-06 | K-406 (waste gas compressor number 4) | Cause: K-406 unexpectedly shut down and waste gas was automatically diverted to refinery safety flare system. Followup: No Notes: Sweet streams (lower Sulfur content) were routed to the flare to minimize sour gas flaring. Process unit output was adjusted in order to minimize the total amount of waste gas being sent to the flare. Shortly after shutdown, personnel re-started K-406 restoring the systems ability to process available refinery waste gas streams, ending the incident. | 14.0 pounds |
| 103126 2008-02-17 | Flare | Cause: conducting functionality test for acid evacuation system. On of vent valves opened to flare. Followup: No Notes: Letter states that emissions were BRQ. | 60.0 pounds |
| 102953 2008-02-08 | No information given | Cause: pump seal failed on G8111 at the #2 Coker causing a fire Followup: No Notes: Letter states that emissions were BRQ. | |
| 123040 2010-04-27 | flare #1 | Cause: Compressor inadvertently tripped while executing Emergency Block Valve Prevention Maintenance Program procedure on it--sent material to flare. Followup: No Notes: Operations team secured the unit and started up the compressor, full evaluation and troubleshooting will be addressed during next shutdown. Will not perform EBV maintenance program in the meantime. |
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