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Chalmette Refining, LLC, Chalmette

Releases of Sulfur Dioxide

LDEQ Incident Number
Incident Date
Point Source(s) Notes Amount of Release
84794

2005-12-24
Rich DGA Pump G-8291
Cause: Electrical supply malfunction caused the auto shutdown of the refinery Sulfur Recovery Unit Train 2. The shutdown resulted in routing of refinery acid gas to the flare system.

Followup: No

Notes: Operations were conducted in order to minimize emissions while maintaining a safe and orderly stabilization of refinery operations and restart of the impacted process unit. Repairs were made to applicable electrical equipment and SRU train 2 was restarted, ending the incident. The refinery has initiated an investigation into the cause of this incident. Based on the result of that investigation, appropriate measures will be taken in order to prevent a recurrence due to the same cause.
103,560.0 pounds
84723

2005-12-22
Dip-leg of SRUTR1
Cause: Unit shutdown, during shutdown and hot stand-by of the unit emissions occur via the THOX.

Followup: No

Notes: Operations were conducted in order to minimize emissions while maintaining a safe and orderly shutdown of the impacted unit. The refinery has initiated an investigation into the cause of this incident. Based on the result of that investigation, appropriate measures will be taken in order to prevent a recurrence due to the same cause.
33,375.0 pounds
84745

2005-12-22
Sulfur Recovery Unit Train 2
Cause: instrument malfunction caused the automatic shutdown of the refinery sulfur recovery unit train 2, resulting in the routing of refinery acid gas to the flare system (No. 1)

Followup: No

Notes: Operations were conducted in order to minimize emissions while maintaining a safe and orderly stabilization of refinery operations and restart of the impacted process unit. Repairs were made to applicable instrumentation and SRU Train 2 was restarted, ending the incident. The refinery has initiated an investigation into the cause of this incident. Based on the result of that investigation, appropriate measures will be taken in order to prevent a recurrence due to the same cause.
381,000.0 pounds
84684

2005-12-20
No information given
Cause:

Followup: No Information Provided

Notes: This is a notice rescinding the
77.0 pounds
05-BB005-297

2005-12-18
Coker 2 Wet Gas Compressor K8101
Cause: Compressor went into high alarm for high vibration. It was determined that the vibration probe had provided a false alarm due to a faulty connection.

Followup: No

Notes: In order to avoid equipment damage and associated emissions, refinery personnel shut down the machine. The vibration probe was repaired and the machine was put back in service, ending the incident. Instrument and electrical connections directly relatedto K8101 were double checked for proper connections in order to avoid a recurrence due to the same root cause.
26,127.0 pounds
84474

2005-12-12
Wet Gas Compressor K8101
Cause:

Followup: No

Notes: Machine restarted. Below reportable quantities
632.0 pounds
84328

2005-12-05
Operating Sulfur Recovery Unity
Cause: Loss of power triggered upset of refinery and shutdown of the refinery's operating sulfur recovery unit.

Followup: No

Notes: Operations were conducted in order to minimize emissions while maintaining a safe and orderly stabilization of refinery operation and restart of some refinery process units. Refinery Management has met with Entergy to stress the impact of this incident and request that appropriate measures be taken in order to prevent a recurrence.
900,344.0 pounds
84073

2005-11-23
No. 2 Coker Wet Gas Compressor
Cause: The wet gas compressor shut down due to the axial thrust alarm, resulting in emissions from the No. 1 Flare. Following investigation, refinery personnel believe the Wet Gas Compressor shut down due to a momentary loss of lube oil.

Followup: No

Notes: In an effort to stop the release, the compressor was restarted, but the alarm remained. Following determination by refinery personnel that maintenance was required on the compressor, K-8101 was taken out of service and sent out for repair. A variance was applied for with the LDEQ to authorize the emissions associated with the compressor maintenance. The variance was approved on November 29, 2005, ending this release.
255,680.0 pounds
05-BB005-280

2005-11-21
No. 2 Crude Unit Prefractionator (Prefrac) Tower
Cause: Pressure spikes on the No. 2 Crude Unit Prefractionator Tower coupled with increased Overhead Accumulator levels, and problems maintaining tower bottoms circulation. The tower pressure exceeded the process relief valve set pressure, ad the Prefrac Towerrelieved to the No. 2 Flare resulting in Sulfur Dioxide emissions in excess of reportable quantity.

Followup: No

Notes: In an effort to stop the release, bypasses were opened o the water boot level controllers on both the Atmospheric and Prefrac Towers, and the Prefrac Overhead fin-fans were started. Prefrac Bottoms product was slopped due to water content and the Stabilizer Tower was also shutdown. Following determination by Refinery Personnel that the problem was due to a false Prefrac Bottoms level indication, the level was dropped by increasing the flow to slop, returning tower operation to normal. The level tritter is scheduled for repair in order to reduce the likelihood of a recurrence.
841.0 pounds
05-BB005-281

2005-11-21
Sulfur Recovery Unit Thermal Oxidizer Stack
Cause: Refinery personnel diverted acid gas from Train I of the SRU due to mechanical issues on the unit. Diverting the acid gas resulted in Sulfur Dioxide emissions from the Thox stack in excess of the permit limit, resulting in a reportable release.

Followup: No

Notes: Sulfur dioxide to atmosphere through the SRU Thox Stack.
8,632.0 pounds
83924

2005-11-17
Hydrodesulphurization (HDS) Unit Fans
Cause: Leak on the HDS Unit fans caused spill to the ground. Emissions resulted from the spill to the ground, the release to the atmosphere and from the unit de-pressure to the No. 2 flare.

Followup: No

Notes: Chalmette Refinery rescinded the 11/17/05 notifications for NO, NO2, VOC, SO2 and H2S since the estimated amounts were less than the reportable quantity of 10lbs. Calculations performed after the incident indicated that a greater than reportable quantity of oil was spilled to the ground during this incident.
783.0 pounds
05-BB005-267

2005-08-27
Plant Facility
Cause: Shutdown in advance of Katrina. Emissions resulted from gas flaring, fuel gas quality changes, and standby operation modes necessitated by the shutdown.

Followup: No

Notes: Substance released to atmosphere through the refinery. For the refinery shutdown, operations were conducted in order to minimize emissions while maintaining a safe and orderly shutdown.
34,400.0 pounds
81016

2005-08-05
Coker 1 Heavy Gas Oil pump G2804 problem led to release at the No. 2 Flare
Cause: Seal on coker 1 Heavy Gas Oil pump G2804 failed, causing a localized fire at the pump. Caused coker 1 wet gas compressor K2800 to shutdown due to high drum level. Flare to no. 2.

Followup: No

Notes: Unit throughput was reduced to minimum and attempts to restart required process equipment were made. Unit feed was changed from sour (high H2S concentrations) to sweet (lower H2S concentrations) to minimize emissions. The unit was stabilized and the flaring ceased.
6,968.0 pounds
80865

2005-07-22
Hydrocracker
Cause: Hydrocracker overpressured

Followup: No

Notes: BELOW REPORTABLE QUANTITIES
4.0 pounds
05-BB005-243

2005-07-17
Wet Gas Compressor K 2800 shut down and went to the No. 2 Flare
Cause: coker 1 wet gas compressor (K2800) shut down due to high knock-out drum level. Resulted in flaring of process gasses until it could be re-started.

Followup: No

Notes: Process adjustments were made in order to minimize the likelihood of fractionators liquid carryover and high knock-out level, prior to the re-start of the compressor. K2800 was re-started, ending the incident
155.0 pounds
80566

2005-07-16
Hydrodesulphurization (HDS) Unit problem went to No. 2 Flare
Cause: Leak in the HDS

Followup: No

Notes: The unit was shut down so that the leak could be isolated and repaired.
1,126.0 pounds
80502

2005-07-13
Transformer power outage - emitted at No. 2 Flare
Cause: Loss of a refinery power transformer resulted in unplanned shut-down of coker 1, resulting in flaring to no. 2

Followup: No

Notes: backup transformer was placed in service to replace the one that failed.
1,096.0 pounds
80322

2005-07-06
No information given
Cause:

Followup: No

Notes: Tropical storm caused power failure
50,599.0 pounds
80291

2005-07-04
No information given
Cause:

Followup: No

Notes: rescind notification
309.0 pounds
79721

2005-06-09
Compressor K-2800
Cause: Overfill of lube oil reservoir resulted in compressor K-2800 tripping offline. Off gas was routed to the no. 2 flare.

Followup: No

Notes: reservoir level lowered and compressor restarted. Additional training conducted to ensure operator is always observing filling.
538.0 pounds
79189

2005-05-19
Hydrocracker Light Ends Plant - Butane Splitter Tower
Cause: : Excess feed to the Depropanizer Tower caused overpressure

Followup: No

Notes: moves to reduce temperature and pressure were made in effort to prevent the depressurization of the Butane Splitter to the refinery flare system. Cooler back flushing was conducted in order to ensure that maximum cooling was available, heater firing wasreduced in order to reduce tower temperatures and pressures.
1,176.0 pounds
79008

2005-05-11
K7402 No. 2 Crude Unit
Thermal Oxidizer Stack on the API
Cause: Gas oil tower overhead compressor tripped

Followup: No

Notes: Below reportable quantities
189.0 pounds
05-BB005-210

2005-05-11
K3304
Cause: Leak on the Hydrodesulphurization (HDS) Unit Off0gas Compressor K-3304

Followup: No

Notes: Sweet streams (lower Sulfur content) were routed to the flare to minimize sour gas flaring. Process unit output was adjusted in order to minimize the total amount of waste gas being sent to the flare.
31.0 pounds
05-BB005-205

2005-05-05
No information given
Cause:

Followup: No

Notes: Below reportable quantities
402.0 pounds
78760

2005-05-02
K7702 Cat Feed Hydrotreater
Cause: Cat Feed Hydrotreater make-up compressor automatically shut down due to thermal overload. The shutdown caused excess acid gas loading at the refinery Sulfur Recovery Unit (SRU) which lead to increased Sulfur Dioxide emission from the SRU Thermal Oxidizer (THOX)

Followup: No

Notes: K7702 was restarted and SRU and CFHT operations were stabilized and efforts were made to reduce SRU THOX Sulfur Dioxide concentrations
856.0 pounds
78674

2005-04-29
Coke drum
Cause: Coke drum got too hot, causing gases to be sent to flare

Followup: No

Notes: Below reportable quantities
78541

2005-04-26
Sulfur Recovery Unit, Hydrocracker, #2 Coker, #2 Crude
Cause: A loss of power to the Refinery's Boiler Instrumentation System caused the shutdown of the three plant boilers which generate the Refinery's 600 lb. steam. The loss of 600 lb. steam production caused upset conditions at a series of Refinery Process Units including the Sulfur Recovery Unit, Hydrocracker, #2 Coker and #2 Crude

Followup: No

Notes: The refinery has initiated an investigation into the cause of this incident. Based on the result of that investigation, measures will be taken in order to prevent a recurrence due to the same cause
78,817.0 pounds
78361

2005-04-19
K-401 (waste gas compressor number 2)
Cause: Waste gas compressor number 2 (K-401) automatically shut down, automatically diverting waste gas to the flare system.

Followup: No

Notes: Low-Sulfur content streams were routed to the flare to minimize sour gas flaring. Output was adjusted to minimize total amount of waste being sent to the flare. Same language about doing an investigation to understand the underlying cause and prevent future incidents.
970.0 pounds
78345

2005-04-18
No information given
Cause: Compressor tripped offline

Followup: No

Notes: Below reportable quantities
332.0 pounds
78341

2005-04-17
K-401 (waste gas compressor number 2)
Cause: Waste gas compressor number 2 (K-401) automatically shut down, automatically diverting waste gas to the flare system.

Followup: No

Notes: Low-Sulfur content streams were routed to the flare to minimize sour gas flaring. Output was adjusted to minimize total amount of waste being sent to the flare.
707.0 pounds
78226

2005-04-13
K-401 (waste gas compressor number 2)
Cause: Waste gas compressor number 2 (K-401) automatically shut down, automatically diverting waste gas to the flare system.

Followup: No

Notes: Low-Sulfur content streams were routed to the flare to minimize sour gas flaring. Output was adjusted to minimize total amount of waste being sent to the flare. Letter rescinds report of nitric oxide because below reportable quantity.
2,161.0 pounds
05-BB005-157

2005-04-06
K-402 (Refinery waste gas compressor number 3)
Cause: K-402 unexpectedly shut down. Shortly after shutdown, refinery personnel identified the cause of the shutdown as a malfunction of the compressor motor ignition system.

Followup: No

Notes: The compressor motor was repaired and the compressor restarted, ending the incident.
33,873.0 pounds
77936

2005-03-31
K-400 (Refinery waste gas compressor number 1)
Cause: Refinery waste gas compressor number 1 (K-400) unexpectedly shut down. Refinery waste gas automatically diverted to the flare system.

Followup: No

Notes: Adjustments made to the fuel/air mixture and K-400 restarted.
706.0 pounds
77659

2005-03-17
No information given
Cause: Waste gas compressor number 2 (K-401) automatically shut down due to a high temperature.

Followup: No

Notes: Letter rescinds verbal report because incident was not reportable. No release to atmosphere.
77659

2005-03-17
No information given
Cause: Waste gas compressor number 2 (K-401) automatically shut down due to a high temperature.

Followup: No

Notes: Letter rescinds verbal report because incident was not reportable. No release to atmosphere.
888.0 pounds
05-BB005-135

2005-03-13
C-2307 (Second Stage High-Pressure Separator) level controller; K-2303 (HCU Second Stage Recycle Compressor)
Cause: During maintenance, the Hydrocracker (HCU) Second Stage High-Pressure Separator (C-2307) level controller was inadvertently left in the manual position. Later, HCU Second Stage Recycle Compressor (K-2303) shut down due to high level in C-2307. Shutdown of K-2303 caused automatic depressurization of C-2307 to the refinery flare system.

Followup: No

Notes: Letter rescinds report of Sulfur Dioxide because below reportable quantity.
12.0 pounds
05-BB005-128

2005-03-02
Waste Gas Compressor Number 4 (K-406); Copper tubing connecting C-435 (first stage suction drum) to high-level instrumentation
Cause: Waste gas compressor number 4 (K-406) shut down due to failure of piece of copper tubing connecting C-435 to high-level shutdown instrumentation. When it failed, a false high level reading was recorded, causing automatic safety shutdown system to become engaged.

Followup: No

Notes: Low-Sulfur content streams were routed to the flare to minimize sour gas flaring. Output was adjusted to minimize amount sent to the flare. C-435 was retubed, K-406 was checked and restarted.
6,322.0 pounds
76869

2005-02-11
No information given
Cause: From the verbal report:

Followup: No

Notes:
454.0 pounds
05-BB005-113

2005-02-07
Unintended over pressurization of the Hydrocracker Light Ends Plant (HCU LEP) Depropanizer surge drum
Cause: Due to the isolation of the sight glass of the hydrocracker light ends plant depropanizer, the automatic level indication equipment was disabled and false reading was transmitted; this condition caused an unintended over pressurization of the HCU LEP Depropanizer surge drum, which was venter to the refinery flare system (No. 2 flare)

Followup: No

Notes: Refinery personnel evaluated the process operation, identified the source of the problem and made appropriate corrections, ending the incident.
401.0 pounds
05-BB005-106

2005-02-04
Electrical breaker G-457; Waste gas compressor number 2 (K-401)
Cause: Electrical breaker for G-457 malfunctioned. Waste gas compressor number 2 (K-401) shut down as a result of the electrical power outage and refinery waste gas was diverted to safety flare system.

Followup: No

Notes: Low-Sulfur content streams were routed to the flare to minimize sour gas flaring. Output was adjusted to minimize total amount of waste being sent to the flare. Note: the breaker for G-457 had been identified for repair and was supposed to be replaced that week.
4,075.0 pounds
05-BB005-100

2005-01-24
Waste gas compressor shut down and caused an over pressure situation
Cause: From the verbal report:

Followup: No

Notes:
05-BB005-93

2005-01-22
K-406 (waste gas compressor number 4)
Cause: Waste gas compressor number 4 (K-406) unexpectedly shut down. Waste gas was automatically diverted to refinery safety flare system.

Followup: No

Notes: Note: This compound was not included in the body of the letter. It was listed in a chart attached to the letter.
4,543.0 pounds
76362 & 76355

2005-01-21
Hydrocracker Light Ends Plant Butane Splitter Tower & LEP Depropanizer Tower Bottoms Flow Control Valve 50FC060
Cause: (1) 0600 hrs: Hydrocracker Light Ends Plant (LEP) Butane Splitter Tower began to overpressure because LEP Depropanizer Tower Bottoms Flow Control Valve (50FC060) had failed in the open position, letting propane to exit to the Butane Splitter. (2) 1700 hrs: Butane Splitter again began to overpressure due to the presence of propane. The level indication on the level instrument was detecting a false reading.

Followup: No

Notes: Letter speaks of two incidents on same day at 0600 hrs and 1700 hrs but attached report shows three incidents: (1) 4:05 a.m. lasting 3h 42m; (2) 3:15 p.m. lasting 41m; (3) 4:30 p.m. lasting 1h 25m. Amounts of compounds are only given in totals for all 3incidents.
4,589.3 pounds
76224

2005-01-18
No information given
Number 2 Flare -- Pressure Safety Valve (PSV) on Fuel Drum for Number 10 Boiler
Cause: From the verbal report:

Followup: No

Notes:
2.0 pounds
05-BB005-67

2005-01-06
K-406 (waste gas compressor number 4)
Cause: K-406 unexpectedly shut down and waste gas was automatically diverted to refinery safety flare system.

Followup: No

Notes: Sweet streams (lower Sulfur content) were routed to the flare to minimize sour gas flaring. Process unit output was adjusted in order to minimize the total amount of waste gas being sent to the flare. Shortly after shutdown, personnel re-started K-406 restoring the systems ability to process available refinery waste gas streams, ending the incident.
726.0 pounds
92940

2006-12-29
Waste Gas Compressor
Cause: Waste Gas System Compressor shut down due to water contamination of the oil in the crank case.

Followup: No

Notes: Rates at the HDS and CFHT units were reduced and CRLLC routed sweet hydrocarbons streams to the flares to minimize flaring. Oil was drained from the crank case and replaced. The K-406 Compressor was restarted.
31,282.0 pounds
92642

2006-12-14
Flare No. 2 EPN 29
Cause: Crude 2 K-7601 Compressor shut down

Followup: No

Notes: Machinists restarted the compressor and an investigation of the incident is underway.
3,236.0 pounds
92491

2006-12-08
Number 2 Flare
Cause: Under investigation

Followup: No

Notes: Relief valve will be inspected; Pressure was lowered on First Stage Stripper. The inlet block valve was closed and flow to the #2 Flare stopped, ending the incident. The block valve was reopened.
2.0 pounds
92484

2006-12-08
Number 1 Flare AE-AOA-05-0109 EPN 28
Cause: valves were misaligned in the field leading to acid gas being sent to #1 Flare

Followup: No

Notes: refinery has reviesed the procedure for switching a SRU tran to acid gas and will train unit operators on the revised procedures.
2,988.0 pounds
92464

2006-12-07
Lube Oil Cooler on Waste Gas Compressor K-406
Cause: leak in lube oil cooler tubing on WGC

Followup: No

Notes: Lube oil cooler on compressor was shut down. Leaking cooler tubing was repaired and all of the tubing was hydro-tested.
92469

2006-12-07
Lube Oil Cooler on Waste Gas Compressor K-406
Cause: leaking lube oil cooler on WGC

Followup: No

Notes: Letter written to rescind notification of 12/7/6
92440

2006-12-05
#2 Flare - AE-AOA-05-0109 EPN 29
Cause: Quench pump G-7621 was down which increased gas production and caused a sudden increase in off gas from crude 2 vacuum tower.

Followup: No

Notes: Unknown why quench pump was down. Will install a switch guard to prevent unintentional shutdown.
5,505.0 pounds
92412

2006-12-04
#1 Flare
#2 Flare
Cause: shut down of interstage cooler causing trip of WGC

Followup: No

Notes: Resetting alarms to appropriate levels; reinforced training of the operators on WGS operations at low temperatures.
1,946.0 pounds
92394

2006-12-02
#1 Flare AE-AOA-05-0109 EPN 28
#2 Flare - AE-AOA-05-0109 EPN 29
Cause: WGCs K-402 and 406 tripped due to an instrument air leak on the K-402 control panel. Leak was fixed and WCGs turned back on

Followup: No

Notes: Investigation ongoing.
19,224.0 pounds
92383

2006-12-01
AE-AOA-05-0109 EPN 28
Cause: WGC (K-8101) tripped due to low seal Oil pressure. Main pump was shut down due to erratic operation due to wet steam. WGC restarted ending incidend. Liquid level indicator in the GRU condensate drum was not working.

Followup: No

Notes: put in work order for liquid level indicator.
722.0 pounds
92194

2006-11-21
#1 Flare - AE-AOA-05-0109 EPN 28
#2 Flare
Cause: Compressor K-406 tripped for unknown reasons.

Followup: No

Notes: Under investigation.
3,723.0 pounds
92158

2006-11-18
#1 Flare - AE-AOA-05-0109 EPN 28
Cause: WGC K-406 tripped due to high vibrations. The shutdown caused the pressure in the WGS to increase and hydrocarbon gas with Hydrogen Sulfide was routed to the number 1 flare

Followup: No

Notes: cause of vibration is unknown at this time. K-406 will be inspected for damage.
4,607.0 pounds
92095

2006-11-15
AE-AOA-05-0109 EPN 28
Cause: FCC tripped due to a blown fuse and a malfunctioning component within the FCC multi lin and fuse system. A second mechanical failure (currently under investigation) dropped the remaining voltage to below the sct point.

Followup: No

Notes: Investigation ongoing. Unit feed rates reduced to a minimum and reactor severity was reduced. In addition, moves were made to minimize the main fractionators overhead receiver pressure. Process gas was routed to the #1 Flare while troubleshooting was performed.
8,190.0 pounds
91667

2006-10-29
AE-AOA-05-0109 EPN 28 and 29
Cause: electrical switchgear failure.

Followup: No

Notes: DEQ report indicates that unknown amounts of the pollutants were released.
22,226.0 pounds
91457

2006-10-17
AE-AOA-05-0109 EPN 29
Cause: release occurs during major turn around of refinery. Planned system outages created higher than usual operating pressure on the WGS and AMU. Additionally, on 10/13, the stream was re-routed (misaligned) through a line with an unidentified check valve. Subsequent attempts to push liquid through the AMU line resulted in increased pressure on the WGS.

Followup: No

Notes: Investigation ongoing. PSV set pressure was raised to allow for higher head pressure events at WGS without flaring. Detailed investigation ongoing.
30.0 pounds
91273

2006-10-10
Thermal Oxidizer and Flare 1 - AE-AOA-05-0109 EPN 46
Cause: Discharges came from THOX and Flare 1. The Amine and Sulfur Recovery Units were upset. It was determined that hydrocarbons contaminated the Diglycolamine (DGA¨) and required both units to be taken offline. The upset caused excess emissions from the SRU 1 Thermal Oxidizer (THOX). Sulfer Plant feed was diverted to the refinery safety flare system while the conditions which cause the upset were isloated and remedied. CRLLC reduced the rates of acid gas productin units to minimum and lowered total sufer content of remaining feed, within refinery capability.

Followup: No

Notes: CITIZEN COMPLAINT COINCIDES WITH INCIDENT - all acid gas producing units were cut back to minimum rates. The source of hydrocarbon in the DGA system was isolated and then purged. The refinery has initiated an investigation into the cause of this incident. Based on the result of that investigation, appropriate measures will be take in order to prevent a recurrence dut ot the same cause.
1,068,405.0 pounds
90624

2006-09-12
#1 Flare - AE-AOA-05-0109 EPN 28
Cause: No information given

Followup: No

Notes: Letter written to rescind notification of 9/12/6
90535

2006-09-08
#1 Flare - AE-AOA-05-0109 EPN 28
Cause: during Coker 1 startup the top of the fractionator tower flooded due to an unstable flow from the heavy gas Oil pump around (typical during startup). The end result was an overpressure to the emergency flare system.

Followup: No

Notes: the k-2800 will be reconnected to the Number 2 Flare for use in emergency situations only until the FGR System is commissioned. Communication to employees on what constitutes and emergency situation will occur.
1,005.0 pounds
90486

2006-09-06
#1 Flare - AE-AOA-05-0109 EPN 28
Cause: Flooding in the Crude 2 Gas Oil Tower caused by a false reading from a level controller (74LC503). Ultimately lead to backflush and overpressure.

Followup: No

Notes: Flushing medium valve was reopened. Process adjustments were made to restore product quality for Crude 2 to the CFHT. Distillate quench was added to cool down the FCCU regeneration bed temperature.
800.0 pounds
90319

2006-08-29
No information given
Cause: No information given

Followup: No

Notes: Letter written to rescind notification of 8/29/06
37.0 pounds
89699

2006-08-03
AE-AOA-05-0109 EPN 29
Cause: gas compressor tripped due to a sudden change in feed composition and or compressor suction pressure

Followup: No

Notes: refinery has initiated an investigation into the cause
695.0 pounds
84697

2006-08-02
AE-AOA-05-0109 EPN 46
Cause: loss of instrument air pressure resulting in upset and shutdown of multiple process units within the refinery. Resulted from July 31, 2006 upset and the resultant restart and passivation of SRU Train 2

Followup: No

Notes: refinery has initiated an investigation into the cause
3,173.0 pounds
89716

2006-08-02
AE-AOA-05-0109 EPN 46
Cause: No information given

Followup: No

Notes: This incident tied to 84697. Both listed in same incident report from CRLLC.
89604

2006-07-31
AE-AOA-05-0109 EPN 46
Cause: loss of instrument air pressure resulting in upset and shutdown of multiple process units within the refinery

Followup: No

Notes: Process adjustments were made to restore refinery instrument air and steam systems. Process units were stabilized, ending the incident.
7,184.0 pounds
89597

2006-07-29
No information given
Cause: loss of flow in the tail gas compressor

Followup: No

Notes: Letter written to rescind notification of 7/29/06
46.0 pounds
89555

2006-07-27
No information given
Cause: upset on amine unit.

Followup: No

Notes: Letter written to rescind notification of 7/27/06
25.0 pounds
89470

2006-07-21
SRU Thermal Oxidizer Stack
Cause: inadequate oxygen flow to SRU2 due to lack of manual adjustments by refinery personnel

Followup: No

Notes: LDEQ was not notified of the release within the 24 hour nonemergency notification period. Process adjustments were made to bring the unit back on ratio.
1,577.0 pounds
89255

2006-07-13
AE-AOA-05-0109 EPN 46
Cause: section circulation impeded when an exchanger is plugged resulting in diversion from train 2 to train 1

Followup: No

Notes: Repairs to Train 2 MDEA Lean/Rich Exchanger (E8062) are being scheduled in order to return Train 2 tail gas section to service.
1,136.0 pounds
89525

2006-06-26
No information given
Cause: No information given

Followup: No

Notes: Letter written to rescind notification of 6/26/06
46.0 pounds
89431

2006-06-21
#2 Flare AE-AOA-05-0109 EPN 29
Cause: alarm was improperly set allowing motor to operate above its design load leading to shut down of #1 Coker WGC

Followup: No

Notes: K-2800 high amperage alarm has been reset to 208 amps.
2,287.0 pounds
88492

2006-06-11
#2 Flare - AE-AOA-05-0109 EPN 29
Cause: thermal overload from direct sunlight, automatic shut down of WGC

Followup: No

Notes: temporary roof installed over the motor starter / thermal load protection system. This will prevent direct sunlight from contributing to excess temperature on the thermal over arm protection system.
2,926.0 pounds
88381

2006-06-07
Flare
Cause: off gas compressor tripped on overload and released to flare

Followup: No

Notes: Letter written to rescind notification of 6/7/06
288.0 pounds
88280

2006-06-02
No information given
Cause: malfunction in a control valve causes a clearing incident

Followup: No

Notes: DEQ report with no corresponding letter from CRLLC
0
88213

2006-05-31
Number 2 Flare
Cause: cracked tubing caused an instrument to malfunction and caused WGC to trip

Followup: No

Notes: The cracked copper tubing was replaced with stainless steel tubing in order to improve durability. The refinery will evaluate installations on the Low Pressure Waste Gas system where copper tubing is utilized for instrument connections and make upgradesto that tubing, if deemed appropriate, during the next unit turnaround.
782.0 pounds
88173

2006-05-28
No information given
Cause: No information given

Followup: No

Notes: Letter states that emissions were BRQ
100.0 pounds
87979

2006-05-19
Process unit
Cause: leak in a fan in a process unit

Followup: No

Notes: No information given
301.0 pounds
87626

2006-05-04
Thermal Oxidizer at SRU Train 1
Cause: tail gas analyzer malfunctioned

Followup: No

Notes: Malfunctioning analyzer was repaired
706.0 pounds
87269

2006-04-19
No information given
Cause: coker compressor failed

Followup: No

Notes: Letter states that emissions were BRQ
346.0 pounds
87236

2006-04-17
No information given
Cause: No information given

Followup: No

Notes: Letter states that emissions were BRQ
378.0 pounds
87121

2006-04-11
AE-AOA-05-010,9AE-AOA-05-0109 EPN 46
Cause: contamination in the air system

Followup: No

Notes: updated unit operating procedures to remove potential impurities from the line prior to future use.
32,624.0 pounds
86878

2006-03-31
Emergency Flare System AE-AOA-05-0109 EPN 29
Cause: waste gas compressors 4 and 3 (K406 and 402) automatically shut down, lowering the refinery capacity and causing overpressure to the emergency flare system. Liquid level pump (G476) switch was in the off position.

Followup: No

Notes: A mechanical guard was placed on the pump switch in order to avoid the unintentional movement of the switch
3,174.0 pounds
86835

2006-03-29
AE-AOA-05-0109
Cause: Plant de-ethanizer tower (2410) relieved pressure to the emergency flare system after that propane treater (C7402) had plugged causing backpressure on the system leading to venting to emergency flare system. Release from Flare no. 2.

Followup: No

Notes: the refinery has initiated an investigation, appropriate measures will be taken in order to prevent a recurrence due to the same cause.
472.0 pounds
86612

2006-03-20
Emergency Flare System AE-AOA-05-0109 EPN 29
Cause: compressor 1(K-400) automatically shut down, lowering waste gas processing capacity and causing overpressure to the emergency flare system. Later, waste gas compressor number 2 (K-401) automatically shut down causing the waste gas system to further overpressure to the emergency flare system.

Followup: No

Notes: the refinery has initiated an investigation, appropriate measures will be taken in order to prevent a recurrence due to the same cause.
2,204.0 pounds
86447

2006-03-13
AE-AOA-05-0109
Cause: loss of power resulted in the unplanned upset of the refinery. External power supplied by Entergy was lost due to activity external to refinery operations. Release from Nos. 1 and 2 Flares.

Followup: No

Notes: Specific action taken: met with Entergy to stress the impact of this incident and request that appropriate measures be taken in order to prevent a recurrence.
680.0 pounds
85834

2006-02-15
Waste Gas Compressor
Cause: process equipment allowed light ends to enter Tank 75 during an upset. The tank vent ignited briefly during this period.

Followup: No

Notes: Letter written to rescind notification of 2/15/06
85837

2006-02-14
No information given
Cause: No information given

Followup: No

Notes: Letter written to rescind notification of 2/14/06
322.0 pounds
85454

2006-01-29
Thermal Oxidizer AE-AOA-05-0109 EPN 46
Cause: steam leak into SRUTR1 prcoess necessitated shutdown and transfer to another unit

Followup: No

Notes: refinery has initiated an investigation into the cause
3,141.0 pounds
101895

2007-12-21
Flare
Cause: upset of FCC; overhead pressure opened to flare

Followup: No

Notes: No information given
101836

2007-12-19
#1 Flare
Cause: #4 Waste Gas system shut down because of misalignment of a sensor and magnetic pick-up. CRLLC technicians also found a bad bearing for the cam shaft idler sprocket.

Followup: No

Notes: Operators immediately tried to start a second compressor. Restarted the shutdown compressor and removed gas flow from flare, ending event.
1,955.0 pounds
101812

2007-12-18
Flare
Cause: power failure caused Reformer #1 to overpressure and vent to flare.

Followup: No

Notes: No information given
101744

2007-12-17
No information given
Cause: #1 prefract loss feed to tower, tower over pressured released SO2

Followup: No

Notes: No information given
101404

2007-12-02
Flare
Cause: compressor problem leads to release to flare

Followup: No

Notes: No information given
101331

2007-11-29
No information given
Cause: #1 prefract loss feed to tower, tower over pressured released SO2

Followup: No

Notes: No information given
101270

2007-11-27
#2 Flare
Cause: frozen material in a pipe prevented material from the HCU and Pretreater to leave towers. Pressure was relieved to flare.

Followup: No

Notes: CRLLC repaired the level gauge and the level transmitter on the De-ethanizer
763.0 pounds
101165

2007-11-19
#2 Flare
Cause: No information given

Followup: No

Notes: No information given
101150

2007-11-18
#1 Flare
Cause: HGO Pump around failed, causing a shut down of #2 Coker Off Gas Compressor

Followup: No

Notes: Operators established the HGO Pump Around before restarting the K-8101 Compressor. When compressor restarted, gas flow removed from flare, ending incident.
4,484.0 pounds
100423

2007-10-22
Emergency Flare System
Cause: Number 1 Coker Wet Gas Compressor shutdown on high amperage when water entrained in the feed line to the compressor caused the compressor to overheat.

Followup: No

Notes: Operators closed the valve to the feed line to the compressor and restarted the K-2800 compressor. The line was again dewatered and lined back up to the compressor K-2800 without shutting down the compressor.
958.0 pounds
100358

2007-10-20
Emergency Flare System
Cause: incident occurred during shut down of the Sulfur Recovery Unit train 1 for maintenance. Train 2 also shut down, initiating release.

Followup: No

Notes: Operators restarted Train 2 twice before they were able to route acid gas through Train 2 and out of the Emergency Flare System ending the flaring.
211,810.0 pounds
100315

2007-10-19
Emergency Flare System
Cause: Train 2 shut down due to low oxygen flow

Followup: No

Notes: Operators restarted Train 2 to end the flaring.
12,020.0 pounds
100171

2007-10-14
#2 Flare
Cause: #2 crude unit prefractionator tower reflux pump tripped

Followup: No

Notes: Letter states that no RQ's were exceeded
100093

2007-10-11
Sulfur Plant
Cause: power failure.

Followup: No

Notes: Letter states that no RQ's were exceeded
99911

2007-10-02
No information given
Cause: No information given

Followup: No

Notes: Letter written to rescind notification of 10/2 concerning release of SO2. DEQ letter indicates there was an SO2 release of 1500 lbs.
99861

2007-09-30
No information given
Cause: pressure safety valve release

Followup: No

Notes: Letter from CRLLC states that no RQ's were exceeded; DEQ letter estimates that there was a release of 2718 lbs of SO2
99870

2007-09-30
#2 Flare
Cause: pressure safety valve release

Followup: No

Notes: Letter states that no RQ's were exceeded
99557

2007-09-18
#1 Flare
Cause: Malfunctioning FCC PGC seal oil level controller. I/E was requested. While I/E's were making adj. the compressor shutdown and excess gas was sent to #1 flare.

Followup: No

Notes: Compressor was restarted ending the flaring. The seal oil level control was replaced.
1,979.0 pounds
99492

2007-09-16
#1 Flare
Cause: hole in the pipeline

Followup: No

Notes: Letter states that no RQ's were exceeded
98732

2007-08-12
No information given
Cause: No information given

Followup: No

Notes: High SO2 readings at Chalmette Vista site and AAM site. Both CRLLC and CII state normal operations with no malfunctions.
98232

2007-07-29
Flare
Cause: upset on hydrocracker

Followup: No

Notes: No information given
98137

2007-07-24
No information given
Cause: No information given

Followup: No

Notes: High SO2 reading at Chalmette Vista air site
98089

2007-07-22
No information given
Cause: compressor had a problem with the coency of water, unable to carry load, flare staged releasing

Followup: No

Notes: Algiers AAM site had readings of 134 ppb
97897

2007-07-15
No information given
Cause: No information given

Followup: No

Notes: Chalmette Vista ambient air site had high SO2 readings from 7/15=7/17. Voluntary response from CRLLC and CII was that everything was operating normally.
97720

2007-07-09
No information given
Cause: No information given

Followup: No

Notes: High SO2 readings at Chalmette Vista site. CRLLC found no problems within the facility.
97504

2007-06-28
No information given
Cause: No information given

Followup: No

Notes: High SO2 readings at Chalmette Vista site. CRLLC found no problems within the facility.
97457

2007-06-27
Emergency Flare System
South Flare
Cause: LPG recovery compressor shut down on a high interstage level due to a faulty level indicator

Followup: No

Notes: Temporary modifications made to LPG interstage level bridle. A new LPG Interstage level indication and shut down system has been designed and the parts have been ordered.
1,815.0 pounds
97539

2007-06-25
Flare
Cause: LPG Compressor tripped and K-3304 compressor R/V had over pressured resulting in some excess flaring and SO2 emissions

Followup: No

Notes: CITIZEN COMPLAINT.
98127

2007-06-25
Fluidized Catalytic Cracking Unit Process Gas Compressor (FCC) (PGC) -- EPN 28
Cause: The FCC PGC tripped due to a blown fuse that was corroded. Due to the loss of the PGC the overhead vapors were released to the #1 flare.

Followup: No

Notes: Immediate restart was attempted when attempsts to restart failed, feed was diverted from the FCC reactor to m. flaring. Fuses were replaced due to corrosion.
5,471.0 pounds
97334

2007-06-23
Flare
Cause: LPG Compressor tripped and K-3304 compressor R/V had over pressured resulting in some excess flaring and SO2 emissions

Followup: No

Notes: No information given
97329

2007-06-22
No information given
Number 2 Flare
Cause: chain operator on the sour waste gas block valve on the #3 Deoctane Overhead Off-Gas Line failed allowing waste gas to go to flare

Followup: No

Notes: CRLLC repaired the malfunctioned chain operator on the #3 Deoctane Overhead Off-Gas sour waste gas block valve.
509.0 pounds
97329

2007-06-22
No information given
Number 2 Flare
Cause: chain operator on the sour waste gas block valve on the #3 Deoctane Overhead Off-Gas Line failed allowing waste gas to go to flare

Followup: No

Notes: CRLLC repaired the malfunctioned chain operator on the #3 Deoctane Overhead Off-Gas sour waste gas block valve.
495.0 pounds
97235

2007-06-19
No information given
Cause: No information given

Followup: No

Notes: No information given
96950

2007-06-09
No information given
Cause: false reading from DGA flow controller leads to shutdown of Waste Gas System Compressor K-400

Followup: No

Notes: CRLLC will initiate a routine maintenance check of the DGA flow controller transmitter and communicate the need for maintenance to the process personnel and instrument techs.
2,735.0 pounds
96736

2007-06-04
# 2 Flare
Cause: while lining up tower to vent, they opened up & a pocket of light hydrocarbons got into flare line

Followup: No

Notes: Letter written to rescind notification of 6/4 concerning release of SO2
96641

2007-05-30
Number 1 Flare
Cause: failure of the central processing unit within the ignition control system for the engine driver for K-402.

Followup: No

Notes: Central Processing Unit within the ignition control system was replaced
8,132.0 pounds
96498

2007-05-23
EPN 28 - #1 flare
Cause: The HDS unit off-gas compression system pressure valve had relieved causing gas to go to the #2 flare after operators failed to verify a prerequisite step of the off-gas compressor start-up procedure.

Followup: No

Notes: attempted to reduce the discharge pressure of the HDS off-gass compressors by water washing the system. HDS charge rates were reduced.
523.0 pounds
96369

2007-05-20
No information given
Cause: No information given

Followup: No

Notes: SO2 above trigger levels at Algiers AAM site.
See notes.
96304

2007-05-16
Bullet #6
Cause: DEQ report states that the flaring is required, indicating that it is part of normal procedures

Followup: No

Notes: Letter written to rescind notification of 5/16 concerning release of SO2
30.0 pounds
96227

2007-05-15
No information given
Cause: No information given

Followup: No

Notes: Letter written to rescind notification of 5/15 concerning release of SO2, NO, NO2
96051 / 96092

2007-05-10
#1 Flare
Cause: after renovation, a low point develops in flare line. Liquid accumulation is blown to flare during coker cycle blow down.

Followup: No

Notes: Letter written to rescind notification of 5/10 concerning release of SO2. Letter states that NO and NO2 were BRQ. Layout of the flare line is being checked to allow the plant to eliminate the problem
95928

2007-05-05
No information given
Cause: new flare gas recovery system that the compressor tripped on

Followup: No

Notes: Letter written to rescind notification of 5/5 concerning release of SO2. File includes flare assessment report for month of April.
95937

2007-05-04
No information given
Cause: shut the compressor down due to potential for significant refinery upset

Followup: No

Notes: Letter written to rescind notification of 5/4 concerning release of hydrocarbons
95843

2007-05-03
No information given
Cause: small fire starts when hot coke ignites during coking process

Followup: No

Notes: Letter written to rescind notification of 5/3concerning release of VOC
18.0 pounds
95667

2007-04-26
Amine Regeneration System
No information given
Cause: No information given

Followup: No

Notes: Letter sent to rescind notification of 4/26 concerning release of SO2
75.0 pounds
95689

2007-04-26
No information given
Cause: No information given

Followup: No

Notes: Letter written to rescind notification of 4/26 concerning release of SO2
499.0 pounds
95667

2007-04-26
Amine Regeneration System
No information given
Cause: No information given

Followup: No

Notes: Letter sent to rescind notification of 4/26 concerning release of SO2
75.0 pounds
95622

2007-04-25
No information given
Cause: No information given

Followup: No

Notes: DEQ voluntarily investigates site and takes SO2 readings. According to the report, the Chalmette Vista site had the highest 24hr average of SO2 that LDEQ has seen to date. There were 10 hrs of readings over 100 ppb with a final 24 hr avg of 108 ppb. The highest hourly reading was 248 ppb.
See notes.
95652

2007-04-25
No information given
Cause: No information given

Followup: No

Notes: Letter sent to rescind notification of 4/25 concerning release of SO2, NO, NO2, H2S,
186.0 pounds
95360

2007-04-15
Sox Scrubber Stack
Cause: see notes. the FCC gas expander triggered a shutdown of the FCC. The pressure in the unit discharged to the atmosphere via the Sox scrubber stack.

Followup: No

Notes: Letter sent to rescind notification concerning release of SO2 and PM. Cleared the valves of catalyst. Expander was restarted at a reduced rate.
265.0 pounds
94950

2007-03-28
#2 Flare
Cause: No information given

Followup: No

Notes: Letter sent to rescind notification of 3/28/07 concerning release of SO2
425.0 pounds
94692

2007-03-18
Gas Recovery Unit - # 1 flare
Cause: see notes. #2 coker wet gas compressor and the GRU experienced pressure swings causing the temp. in the comp. to increase and shutdown.

Followup: No

Notes: control valve in the GRU was out of calibration. Control valve was sending false signals to the control room indicating that the valve was 100% open. The valve was replaced.
1,572.0 pounds
94536

2007-03-11
#2 Coker Unit
Cause: see notes. Fire in the #2 Coker Unit.

Followup: No

Notes: Letter sent to rescind notification of 3/11/07 concerning release of SO2
380.0 pounds
94538

2007-03-11
Waste Gas Compressor
Cause: The WGC tripped due to low seal oil pressure

Followup: No

Notes: the charge rates on the #2 coker WGC were cut. The turbine main pump was restarted and is running in parallel with the auxiliary electric pump.
659.0 pounds
94017

2007-02-18
No information given
Cause: No information given

Followup: No

Notes: Letter sent to rescind notification of 1/24/07 concerning release of SO2
93996

2007-02-15
Emergency Flare System
Cause: Under investigation

Followup: No

Notes: Sweet hydrocarbon gas streams were routed to the flare to reduce the flaring of the sour hydrocarbon gas streams. HDS-rate was lowered to reduce the off-gas rate to the WGS.
1,062.0 pounds
93908

2007-02-12
Cat Feed Hdyrotreater Unit (CFHT) / EPN 28
Cause: CFHT shutdown due to a short in the wiring system. The compressor k-7702 had blown a gasket. The unit depressurized through the emergency flare

Followup: No

Notes: Feed to the CFHT was reduced and the k-7702 compressor was manually isolated. The unit was depressurized to the flare system, ending the incident. CRLLC sends another letter indicating on 3/22 indicating that investigation continues and revisions to prior reports are pending the results.
3,249.0 pounds
93700

2007-02-03
Emergency Flare System
Cause: operator adjusted cooling water system, leading to a shut down of the Waste Gas System Compressor K-400

Followup: No

Notes: Sweet hydrocarbon gas streams were routed to the flare to reduce the flaring of the sour hydrocarbon gas streams. The WGS was restarted and reloaded. CRLLC will reinforce training of operators on the impact of adjustments to the cooling water system.
784.0 pounds
07-BB005-482

2007-02-03
Waste Gas Compressor / Emergency Flare System
Cause: The WGS compressor k-400 shutdown due to an operational adj. that caused high jacket water temp. Sour hydorcarbons were detected

Followup:

Notes: Sweet hydrocarbon gas streams were routed to the flare to reduce the flaring of the sour hydrocarbon gas streams. The WGS was restarted and reloaded.
784.0 pounds
93419

2007-01-21
Coker B Drum
Cause: No information given

Followup: No

Notes: Letter sent to rescind notification of 1/21/07 concerning release of VOC and SO2
0
93384

2007-01-19
No information given
Cause: No information given

Followup: No

Notes: Letter sent to rescind notification of 1/21/07 concerning release of SO2
10.0 pounds
93337

2007-01-17
No information given
Cause: No information given

Followup: No

Notes: Letter sent to rescind notification of 1/17/07 concerning release of VOCs and SO2
3.0 pounds
93240

2007-01-11
#2 Flare
Cause: #2 prefractionator tower bottoms level controller malfunctioned causing resulted in venting to #2 flare

Followup: No

Notes: Refinery has issued a work order to repair the Prefractionator Tower bottoms level controller (741C012)
822.0 pounds
07-BB005-469

2007-01-11
# 2 Crude Unit
Cause: #2 prefactionator tower bottom level controller malfunctioned which resulted in venting to the #2 flare

Followup: No

Notes:
93200

2007-01-10
1st Stage Fin Fan E2415 tube
Cause: leak in tube on 1st stage fin fan

Followup: No

Notes: Root cause analysis initiated. Tube has been sent offsite for analysis. Measures will be taken based on result of analysis.
25.0 pounds
93101

2007-01-07
Sulfur Recovery Unit
Cause: the governor control arm was sticking which caused a problem with the blower.

Followup: No

Notes: Initial report indicates emissions were: SO2 - 500 lbs and H2S - 100 lbs, but letter from Chalmette states that further investigation indicates amt released of both substances was 0 lbs. Follow-up letter adjusts emissions to numbers listed here.
433.0 pounds
110843

2008-11-18
#1 Flare
Cause: start up of the alkylation unit

Followup: No

Notes: Letter states that emissions were BRQ.
110391

2008-10-25
#1 Flare
Cause: upset condition in a process unit

Followup: No

Notes: Letter states that emissions were BRQ.
108944

2008-09-12
Flare #2
Cause: Hurricane Ike causes a scaffold to fall and damage a power line. Power outage causes shut down of Crude 1 and Crude 2 Units

Followup: Yes

Notes:
6,180.0 pounds
108882

2008-09-11
No information given
Cause: pressure safety valve released

Followup: No

Notes: No Information Given
No information Given

2008-08-30
Flare
Cause: shutting down units due to hurricane

Followup: No

Notes: All incidents grouped in one report concerning activities surrounding start up and shut down near the arrival of Hurricane Gustav. CRLLC reports requesting a variance for all emissions resulting from these events.
671,171.0 pounds
108453

2008-08-29
No information given
Cause: shutting down units due to hurricane

Followup: No

Notes: Letter states that emissions were BRQ.
108528

2008-08-20
Flare
Cause: shutting down units due to hurricane

Followup: No

Notes: No Information Given
108123

2008-08-16
thermal oxidizer stack
Cause: No information given - train trippedÉhit switch to train oneÉtrain one become overloaded

Followup: No

Notes: Claims emission was below RQ.
108301

2008-08-02
Sulfur Recovery unit THOX stack
Cause: the air demand analyzer became plugged and a breaker was switched off

Followup: No

Notes: Issued a work order to investigate equipment. Unable to confirm if workers bumped the breaker. Reported as a Tail Gas Incident. Letter of 10/24 includes checks to the DoJ and LDEQ as paymt of penalty for incident.
5,454.0 pounds
107279

2008-07-17
Flare
Cause: the level controller on the slurry pump around system malfunction and the FCC fractionator overpressured

Followup: No

Notes: Corrected the level indicator
734.0 pounds
107088

2008-07-09
No information given
Cause: No information given

Followup: No

Notes: Claims emission was below RQ.
105915

2008-05-23
#2 Flare
Cause: excess light material in the feed stream caused the Crude 2 Atmospheric Tower to over pressure. CRLLC began processing a new type of crude that caused the upset.

Followup: No

Notes: CRLLC reduced the Crude 2 Feed rate and made adjustments to the feed rate to reduce the pressure in the atmospheric tower and in the Prefractionator Tower.
922.0 pounds
103974

2008-03-15
No information given
Cause: high winds blew a tarp into a power line; cooling water pumps were lost

Followup: No

Notes: Letter states that emissions were BRQ.
103563

2008-03-01
Emergency Flare System
Cause: operator over-adjusted flow to the inter-stage cooler after receiving a high temperature alarm on the Process Gas Compressor

Followup: No

Notes: When PGC lost suction, the board operator immediately directed the outside gas operator to decrease the cooling water flow. The intercooler temperature returned to normal operating range and the PGC was able to compress and pump the process gases again
1,026.0 pounds
103437

2008-02-26
No information given
Cause: power failure in FCC Unit

Followup: No

Notes: Letter states that emissions were BRQ.
103126

2008-02-17
Flare
Cause: conducting functionality test for acid evacuation system. On of vent valves opened to flare.

Followup: No

Notes: Letter states that emissions were BRQ.
231.0 pounds
102953

2008-02-08
No information given
Cause: pump seal failed on G8111 at the #2 Coker causing a fire

Followup: No

Notes: Letter states that emissions were BRQ.
3.0 pounds
102818

2008-02-04
#2 Flare
Cause: excess light material in the feed stream caused the Depropanizer Tower to experience processing difficulties that resulted in a pressure increase in the Tower.

Followup: No

Notes: Operators reduced the feed rate to the Debutanizer Tower and cut back the production of overhead liquids from other units supplying the Light Ends Plant
1,205.0 pounds
102577

2008-01-25
#2 Flare
Cause: liquid from Crude 2 Stabilizer Overhead Receiver carried over into the Waste Gas System Line and froze, plugging the line and initiating a series of problems.

Followup: No

Notes: CRLLC repaired the level indicator and changed the alarm points on the gas line to the WGS reducing the probability of such an event and enabling faster identification of such an event. The combined activities will prevent future plugging of the line.
1,461.0 pounds
102455

2008-01-19
Flare
Cause: taking a flare out of service because they have to burn product out so they can install blinds

Followup: No

Notes: Letter states that emissions were BRQ.
102436

2008-01-18
Flare
Cause: taking a flare out of service because they have to burn product out so they can install blinds at the FCC

Followup: No

Notes: Letter states that emissions were BRQ.
102088

2008-01-04
No information given
Cause: Vacuum compressor at #1 crude tripped

Followup: No

Notes: Letter states that emissions were BRQ.
118804

2009-10-17
flare #2
Cause: Level indicator in the Light Ends Plant over head had malfunctioned. Causing the #3 Pretreater and Hydrocracker (HCU) 1st Stage Stripper overhead off gas flow to suddenly decrease. This caused the pressure to increase and release emissions through flaring (#2).

Followup: No

Notes: Lowered drum level and stablizied the HCU and PT 3. Repaired indicator by refilling leg with glycerin.
1,172.0 pounds
118643

2009-10-09
Waste Gas Compressor
Cause: Waste Gas Compressor lost high pressure and failed. Sent gas to FLARE #1.

Followup: No

Notes: RQ not exceeded. Flare gas recovery system prevented excessive flaring.
117083

2009-08-06
SRU 1 and 2
Cause: Sulfur Recovery Unit Train (SRU 2) shutdown due to a steam excursion in the refinery. The steam excursion had caused the SRU 2 to shutdown from low boiler water level. The acid gas loading from SRU 2 was added to SRU 1 which caused the emissions. A second incidence occurred when the refinery lost its hydrogen supply from Air Products. This caused the shutdown of the refinery hydrotreaters and a significant decrease in refinery acid gas production. SRU 1 shutdown due to the insufficient acid gas leading to a second emission.

Followup: Yes

Notes: acid gas was routed from SRU 2 to SRU 1. Acid gas flaring was avoided and DGA strippers was contained until SRU 1 was restarted. SRU 1 was run at minimal air flow rates to avoid excess H2S consumption due from insufficient acid gas rates. Caustic addition was maximized in tail gas section to mitigate additional SO2 formation.
1,136.0 pounds
116434

2009-06-12
coker #2 coke pit and fire lanes
Cause: Failure of the coker fines lane pump discharge check valve resulting from accumulated coke fines, which allowed oil from the coker cutting water tank to back flow into the fines lane. Once the oil came in contact with the hot coke in the pit, a fire resulted.

Followup: Yes

Notes: Fire was extinguished with foam. Secondary check valve was installed and a cautionary procedure was developed and implemented.
3,569.0 pounds
115487

2009-06-08
hose from waste water tank
Cause: Contractor pulled cap off of hose leading to a wastewater tank causing sludge to be released.

Followup: No

Notes: RQ not exceeded. Release cleaned up for future disposal.
267.0 pounds
115514

2009-06-07
PSV lift, tanks 9000, 9006, and 9007
Cause: Unscheduled release of PSV lift, tanks 9000, 9006, and 9007.

Followup: No

Notes: RQ not exceeded.
267.0 pounds
114985

2009-05-14
flare
Cause: High differential pressure across gas oil feed filters to Cat Feed Hydrotreater (CFHT) prevented feed from entering the unit. Loss of feed to CFHT combined with malfunctioned level indicator (instrument failure) in hot separator resulted in the total loss of liquid level in the hot separator. This created high pressure vapor from the hot separator that was fed to the fractionator. This result in the overheating and over pressuring of the fractionator and increased gas rates to the fractionator overhead.

Followup: Yes

Notes: RQ exceeded. CFHT rates reduced to a minimum and stopped using propane to minimize temperature and pressure excursions. Level indicator malfunction ocrrected by replacing the anti-freeze.
2,138.0 pounds
114229

2009-04-16
No Information Given
Cause: No Information Given

Followup: No

Notes: Below reportable quantities.
77.7 pounds
113148

2009-03-04
No Information Given
Cause: No Information Given

Followup: No

Notes: Below reportable quantities.
18.7 pounds
112269

2009-01-24
#1 Flare
Cause: No Information Given

Followup: No

Notes: Below reportable quantities.
151.0 pounds
128197

2010-12-16
No Information Given
Cause: LDEQ report states that it is an air release. No information given regarding cause.

Followup: No

Notes: BRQ. According to the follow-up notification letter, this is a courtesy notification. No reportable quantities were exceeded as a result of this release. Refinery equipment was shut down for repairs.
127974

2010-12-04
No Information Given
Cause: Planned and controlled release to shutdown Alky Unit. LDEQ repor states that "according to the 7-day notification report submitted by the facility, no reportable quantities were exceeded as a result of this release. The release is considered a courtesy notification. No further action at this time."

Followup: No

Notes: BRQ. Release is considered a courtesy notification.
126946

2010-10-08
flare
Cause: Flaring due to isolation of a line involved in a prior incident on 10/4/10 -- see incident #126868. Reportable quantity for Sulfur dioxide was exceeded three times during incident, beginning on 10/10/10.

Followup: No

Notes: RQ. "Valve was fully seated to achieve complete isolation." "No chronic or acute health risks are anticipated as a result of this release..."
78,395.0 pounds
126762

2010-09-29
no information given
Cause: This file only has a brief refinery report with no specific info.

Followup: No

Notes: No information given
126163

2010-09-06
FCC regenerator flue gas scrubber vent
FLARE: Flare #1
FLARE: Thox stack, Flare # 1 and 2
Cause: Bus bar short to ground due to unsealed air gaps created a voltage dip which resulted in power loss to multiple units which then had to flare. Pressure imbalance in the FCC regenerator resulted in loss of catalyst through the regenerator flue gas scrubber vent. FLARE.

Followup: Yes

Notes: "To reduce the likelihood of recurrence, sealant was installed between the bus bars and supports in PS 7711 and acoustic inspection is being performed at another power station that was designed and installed by the same contractor." Refinery letter states that "there was no emergency condition related to this release and the resulting community exposures would not be expected to have acute or chronic health impacts."
106,646.0 pounds
125331

2010-08-02
no information given
Cause: SO2 release when system depressurized for maintenance "permitted release, and not a reportable incident"

Followup: No

Notes: no information given
123156

2010-04-30
no information given
Cause: "Waste gas compressor shut down causing SO2 to flare"--no details given. File contains DEQ report only, refinery letter dated 8/17/10 referred to but not included.

Followup: No

Notes: no information given.
123040

2010-04-27
flare #1
Cause: Compressor inadvertently tripped while executing Emergency Block Valve Prevention Maintenance Program procedure on it--sent material to flare.

Followup: No

Notes: Operations team secured the unit and started up the compressor, full evaluation and troubleshooting will be addressed during next shutdown. Will not perform EBV maintenance program in the meantime.
1,359.0 pounds
122546

2010-04-03
no information given
Cause: "Unloading olefin truck--vent line to flare left open"--no details.

Followup: No

Notes: no information given
121183

2010-01-31
no information given
Cause: verbal report states "petroleum coke fire on conveyor." No detailed description in written report. FIRE.

Followup: No

Notes: no information given
120629

2010-01-08
SOX scrubber
Cause: Fluid Catalytic Cracking (FCC) SOX scrubber circulating water pumps failed due to catalyst pluggage.

Followup: No

Notes: RQ. had difficulty dislodging the catalyst--tried switching pumps off & on, using portable air compressor, increased grid wash, FCC charge rate decreased continuing to monitor performance of SOX scrubber
1,956.0 pounds
135438

2011-11-20
#1 Flare
Cause: The flare gas machines lost its pumping ability. The stages on the #1 flare overpressured and burned the gas into the atmosphere. The cause is under investigation.

Followup: No

Notes: Chalmette Refining provided a courtesy notification to your office regarding a release of Sulfur Dioxide on November 20, 2011. After further review, there were no RQ exceedances or permit violations as a result of this event.
135259

2011-11-14
No. 1 Flare
Cause: On November 14, 2011, the high pressure side waste gas compressors were down for scheduled piping replacement. At approximately 1705 hours, the Flare Gas Management (FGM) system compressors stalled, at which time gas that would have been routed to the FGM contractor, was instead routed to the No 1 Flare. The FGM system would have contained the release; however, the FGM seal water was contaminated with hydrocarbon, which is believed to have been a potential result of the Alky Feed PSV overpressure on November 5, 2011 reported under separate cover. The result was intermittent flaring at the No. 1 Flare through November 15, 2011, at 22:01 hours, consequently resulting in emissions of sulfur dioxide in excess of the reportable quantity of 500 lbs.

Followup: No

Notes: The seal water on the FGM compressors was changed out. CRLLC is investigating the root cause of the release. Based on the results of the Refinery's investigation, appropriate measures will be taken to minimize the likelihood of a recurrence.
5,296.0 pounds
135184

2011-11-09
Flare: Flare No. 1
Cause: The low pressure side waste gas compressor shutdown due to a fuel control valve failure. This routed the low pressure side waste gas to the Flare Gas Management (FGM) system.

Followup: No

Notes: The fuel control valve was repaired. The low pressure side waste gas compressor was restarted, and the stream was removed from the FGM system. The seal water on the FGM compressors was changed out. There is no SPOC report and no LDEQ report in the file.
5,484.0 pounds
135138

2011-11-05
No information given
Cause: No information given.

Followup: No

Notes: Chalmette Refining provided a courtesy notification to the LDEQ regarding a release of Sulfur Dioxide on November 5, 2011. After further review, there were no RQ exceedances or permit violations as a result of this event. The release did not cause an Emergency Condition or require Offsite Protective Action.
134471

2011-10-10
FLARE-No. 1 Flare; SRU 1
Cause: There was sudden unexpected loss of O2 supply from Air Products causing SRU1 to immediately shut down. Acid gas (SO2 and H2S) was released intermittently through Number 1 Flare. SRU 1 was sole operating SRU at the time of incident, as SRU 2 was shutdown for maintenance.

Followup: No

Notes: Steam controllers have been repaired and rebuilt. There was also an evaluation of alarm changes to provide more response time. EPA Acid Gas Flaring report included. LDEQ conducted an investigation in response to this incident on 12/8/11.
164,891.0 pounds
134066

2011-09-18
No information given
Cause: Sulfur dioxide released to atmosphere with no RQ/BRQ

Followup: No

Notes: Chalette Refining provided a courtesy notification to your office regarding a release of sulfur dioxide to the atmosphere on September 18, 2011. After further review, there were no RQ exceedances as a result of this event.
133880

2011-09-11
FLARE: Flare No. 1
Cause: A packing leak developed on the seal of the fire eye cleaning device causing it to malfunction during routine maintenance and allowed combustion gases to escape to the atmosphere and shutting down Train 1 of the SRU (Sulfur Recovery Unit) sending acid gases to the FGM. Flared from flare 1 at a reportable quantity of H2S/SO2.

Followup: No

Notes: Unit operations were adjusted to minimize the duration and severity of flaring. The SRU Train 1 was switched to oxygen mode so it could process refinery acid gas. Sulfur pit vents on both trains were opened until SRU 1 could process them. To prevcnt this from happening again a re-engineered fire-eye cleaning tool will be constructed. This is expected to be completed by December 31, 2011. CRLLC will not utilize the fire-eye cleaning tool until modification to the tool has been completed. Two employees received first aid treatment. No chronic or acute health risks are anticipated as a result of this release. There was no emergency condition as a result of this release. NO SPOC or LDEQ report.
36,579.0 pounds
133625

2011-09-01
No information given
Cause: A heavy rain occurred then the sulfur plant started having problems around 1130 hrs. They started seeing emissions. They believe it is due to an instrument malfunction.

Followup: No

Notes: Chalmette Refining LLC provided a courtesy notification to the LDEQ regarding a release of sulfur dioxide to the atmosphere on September 1, 2011. After further review, there were no RQ exceedances or permit violations as a result of this event.
133061

2011-08-11
FLARE: Unspecified location
Cause: A high pressure waste gas flaring system shut down. The flare gas recovery compressor could not handle the load and sulfur dioxide was released into the atmosphere.

Followup: No

Notes: The unit rates were reduced to lower the amounts going to the flare.
132776

2011-07-29
Flare 1
Cause: On 01/28/11, at approximately 9:00am, the amine unit was being taken out of service for a planned maintenance activity. During the course of the shutdown, the DGA circulation in the contactor decreased. The reduced flow occurred concurrent with the loss of the LPG compressor. As a result, there was an H2S breakthrough to the refinery fuel gas system at approximately 1 minute. This event resulted in 86 lbs of excess SO2 emissions.

Followup: No

Notes: Fuel Gas incident- The shift leader recognized the problem within 15 minutes of the start of the event and immediately increased circulation to stop the H2S breakthrough and mitigate the SO2 emissions potential. Updated procedures to ensure shutdown activities include awareness of circulation rate and interaction with other unit operators. Refresher training will be conducted with unit personnel on revised procedure. In a separate event at 12:58am, the flare gas management compressors briefly shutdown due to elevated molecular weight (MW) gas which resulted in increased SO2 emissions from the fired combustion units of 481 lbs excess SO2
567.0 pounds
132721

2011-07-23
Flare
Cause: On July 23, 2011 at approcimately 23:33 hours, a safety valve on the propane/polypropylene mix drum, D9007 relieved to the No. 1 Flare, resulting in intermittent flaring, and consequently resulting in emission of sulfur dioxide in excess of the reportable quantity of 500 lbs. Incident 11-04337 occurring on July 21, 2011 caused a buildup of hydrocarbons in the compressor seal water decreasing the capacity of the compressors which normally have the capacity to contain this volume.

Followup: No

Notes: The seal water on the FRM compressors was changed out as the hydrocarbon buildup contributed to the flaring. Pressure build up in the spheres occurred before the seal water could be changed out in the compressors causing intermittent flaring. The venting could not be delayed as it would have been a process safety issue. Flaring does not normally occur from these procedures.
1,010.0 pounds
132609

2011-07-20
Flare: Unspecified location
Cause: A sphere over pressured and dumped to the flare. Pressure safety valve lifted and went to flare.

Followup: No

Notes: The sphere was isolated away from the flare.
132188

2011-07-09
No Information Given
Cause: Planned unit shutdown for maintenance operations.

Followup: No

Notes: BRQ: According to the Refinery Letter, "unit operations and shutdown timing were adjusted to minimize environmental impact."
1,949.0 pounds
131213

2011-05-13
FLARE-No. 1 Flare; Sulfur Recovery Unit (SRU) Train II
Cause: Air Products, third party oxygen supplier, experienced a malfunction of an emergency safety device. Oxygen supply was lost to Train II of SRU. The Flare Gas Management System shutdown because of acid gas from the DGA strippers. Two follow-up letters dated 10/25/11 and 11/15/11.

Followup: Yes

Notes: Report states that Air Products re-secured a loose control relay and has ordered a new relay that will fit more securely. EPA Acid-Gas Flaring incident report included. Follow-up letters: A new control relay has been obtained and will be installed in Q4 2012 during a planned outage.
117,344.0 pounds
130963

2011-04-27
No. 2 Coker and Cat Feed Hydrotreater (CFHT)
Cause: Unscheduled outages of the No. 2 Coker and Cat Feed Hydrotreater resulted from a temperature change due to operating on combustion air resulted in the release of sulfur dioxide.

Followup: Yes

Notes: RQ. EPA Consent Decree report included. Immediate remedial actions taken: Upstream unit rates were reduced, the Sour Water Stripper unit was shut down, and SRU conditions were adjusted. Further action: 1)Refresher training has been conducted with increased emphasis on the importance of monitoring the No. 1 Converter temperature closely during train transitions to combustion air with pit vapor to prevent recurrence. 2)Procedure to switch from O2-mode to air-mode was modified. 3)MDEA lean loading field testing to be moved to refinery lab, with upgraded analysis procedures 4)Evaluate project to operate SRU units in partial O2-enrichment mode to reduce environmental vulnerability On January 6, 2012 the refinery sent follow-up notification that all action items related to the April 27, 2011 Tail Gas Incident has been completed.
1,150.8 pounds
130697

2011-04-18
Fluid Catalytic Cracker (FCC) Unit
Cause: According to LDEQ, there was "a pump shut down due to a power trip. After thepump shut down, pressure levels built in the absorber column," which resulted in a release of sulfur dioxide.

Followup: No

Notes: BRQ According to LDEQ, "There is a back-up pump in case of emergency where flow was restored during the... flaring." No further information given.
187.0 pounds
129573

2011-03-01
Flare
Cause: Malfunction of the compressor spillback valve. The Fluidized Catalytic Cracker (FCC) main fractionator overhead accumulator pressure control valve (79PC502F) began to open to flare due to a sudden increase in pressure in the accumulator, which led to flaring at the #1 Flare. The sudden pressure increase was the result of a stuck compressor spillback valve.

Followup: No

Notes: Feed rate to the unit was reduced, pressure was reduced and the pressure control valve setpoint was raised. CRLLC has determined the cause of this release to be a malfunction of the compressor spillback valve. The valve has been evaluated by a technician and the pressure control valve setpoints are being reviewed.
1,014.0 pounds
129381

2011-02-23
PSV Valve
Cause: State Police report states a PSV valve may be leaking and that cause of leak is under investigation. LDEQ Report states PSV valve was leaking to flare system.

Followup: No

Notes: BRQ
140083

2012-05-26

Cause: The facility experienced malfunctions when the high pressure waste gas system was shut down in the Coker unit, releasing sulfur dioxide to the flare.

Followup: No

Notes: The high pressure waste gas system had been restored by the time of the LDEQ Incident Report.
5,769.0 pounds
138541

2012-04-03
#1 Flare
Cause: A high molecular weight gas was routed to the flare gas management system, which prevented the compressor from being able to pump the gas and caused the flare to open.

Followup: Yes

Notes: To stop the discharge, feed rate to the unit was reduced, reducing pressure, and eventually ending the release. A representative from Chalmette Refining contacted LDEQ Emergency Response on 4/4/12 when an all-clear was called, also providing the total release quantity of sulfur dioxide. No fire, injuries, or fatalities resulted from this incident
1,022.0 pounds