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| LDEQ Incident Number Incident Date |
Point Source(s) | Notes | Amount of Release |
| 125465 2010-08-05 | FLARE: HCU relief valve(RV-1191); flow control valve (FC-0735); HCU Flare (4-84) | Cause: LDEQ report states that a release of propylene and propane due to an upset in the hydrocracker unit. The facility reported that a relief valve relieved to flare for approximately one minute. Followup: Yes Notes: BRQ. HCU relief valve was repaired and put back in service. No reportable quantities were exceeded as a result of this release. | |
| 122119 2010-03-13 | HCU absorber surge drum PV-829 HCU oil absorber surge drum PV-829 | Cause: Operator on rounds discovered stain on nozzle bottle of vessel of hydrocracking unit. Plug missing, visible vapors, and there is a quarter inch hole leaking. Followup: No Notes: BRQ. Refinery letter states that "final calculations confirm that no reportable quantities were exceeded." Steam lanced the leak initially, then got advice from piping inspectors for leak repair. Repaired with nipple and isolation valve with cap. | |
| 134290 2011-09-29 | Coker Flare FE-401 | Cause: While starting the Coker Jet Pump on 9/29/11 at 6:45pm, the electrical breaker at Motiva's Coking Unit tripped de-energizing the Motor Control Center. Consequently, the Coker Wet Gas Compressor tripped offline therefore resulting in unit flaring and operating in hot circulation mode. Hot circulation mode is an operating mode in which the unit recycles feed at high temperatures. This mode of operation lessens the amount of flaring in comparison to a complete unit shutdown. The initial inspection of the Jet Pump revealed that the auto-transformer serving as a soft start for this pump had failed causing the electrical breaker to trip open. Once repairs were completed, the Coker Unit was safely re-started and flaring stopped. Followup: No Notes: Immediately, Operations placed the furnace F-125 in hot steam standby and brought the Coker Unit into hot circulation mode to prevent additional flaring of non treated gas. Norco maintenance personnel were called out to troubleshoot the trip of the Coker Wet Gas Compressor and related equipment. The auto-transformer was removed from the circuit. Relay coordination was modified in order to protect the new circuit. After troubleshooting, maintenance personnel determined that operations could safely re-start the Coker Process Unit. During this time the Coker Wet Gas Compressor was restarted and flaring stopped. By 12/31/11 a study will be completed to determine whether the auto-transformer can be permanently removed from the system. After this study is completed, a strategy will be created to address the required changes. This action will be completed by 3/31/12. Calculations confirm that the reportable quantity for sulfur dioxide was exceeded as well as the permitted maximum pound per hour emission limits for carbon monoxide, nitrogen oxide, particulate matter, sulfur dioxide, VOC's, 1,3 butadiene, and benzene as a result of the release. | 6.3 pounds |
| 130903 2011-04-28 | Flare: EPN 3-84 | Cause: A leak occurred at HIC-84, along the downstream block valves, allowing nitrogen to enter the column causing a rapid pressure increase. The distilling unit upper crude column became overpressured, and PCV-195 opened the flare to relieve pressure in the column. EPN 3-84 Flare at Shell was used because the Motiva flare was upset and the pilot light was out. Original upset occurred at Motiva DU-5 Crude Unit with a notrogen leak into the Upper Crude Column. Followup: No Notes: The Shell report for the motiva release was dated May 5th, 2010 instead of 2011. | |
| 136650 2012-01-20 | An Alky six-inch pipeline on the north side of OP-1 process gas compressor | Cause: The leak was caused by internal corrosion, and x-ray results revealed pitting at the leak point. Followup: Yes Notes: Upon discovery of the leak, the refinery isolated the six-inch fuel gas piping at both ends. The problematic section of piping was also depressured and taken out of service to stop the leak. The line was prepared for maintenance inspection, from which the cause--internal corrosion--was discovered. On January 27, 2012, the refinery installed an engineered box over the leak point to permanently repair the piping. |
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