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Placid Refining Co., LLC, Port Allen

Releases in 2009

LDEQ Incident Number
Incident Date
Point Source/Release Notes
118307

2009-09-30
Point Source(s):
Sump pump

Pollutant(s):
Diesel Fuel - BRQ
Kerosene - BRQ
#6 Oil - BRQ
Cause: A delay in the automatic start-up of sump pump 839 on Placid's south dock allowed oily material to back up into secondary containment. A previously unknown crack in the secondary containment curb allowed material to seep out and cause a sheen.

Followup: No

Notes: Automatic switches were replaced, and the pump was reset. Also the crack was repaired.
117777

2009-09-06
Point Source(s):
FLARE

Pollutant(s):
Flammable Gas - BRQ
Cause: planned flaring during start up of an unit.

Followup: No

Notes:
117362

2009-08-18
Point Source(s):
#2 Sulfur Recover Unit

Pollutant(s):
Sulfur Dioxide - 1,054 pounds
Cause: Water got into the instrument air system which resulted in the diversion of acid gases to the number three sulfur unit that resulted in the excess emissions from the #2 Sulfur Recover Unit.

Followup: No

Notes: Police report only. No letter or follow up from the refinery.
116624

2009-07-21
Point Source(s):
FLARE

Pollutant(s):
Sulfur Dioxide - BRQ
Cause: Water from the farm tank reached the crude unit, that result in flaring of preflash gas.

Followup: Yes

Notes: No Information Given
116433

2009-07-09
Point Source(s):
Flare

Pollutant(s):
Sulfur Dioxide - 1,100 pounds
Cause: The released has been happened as a result of flaring during unplanned FCCU shutdown. On 7/9/09 FCCU experienced an uninterruptible power supply malfunction causing an emergency shutdown valves to go into fail position and flared sour water and wet gas.

Followup: No

Notes: No information given. The release has be contained within few hours.
116009

2009-06-25
Point Source(s):
Flare

Pollutant(s):
Sulfur Dioxide - 940 pounds
Cause: Placid#3 sulfur unit experienced a malfunctioning PLC due to overheating. Resulting in the flaring of acid gas and sour water.

Followup: No

Notes: Placid installed a cooler on the PLC panel.
115997

2009-06-25
Point Source(s):
Flare stack, EQT016, EPN 18-74

Pollutant(s):
Sulfur Dioxide - 10,520 pounds
Cause: No. 3 sulfur unit experienced a malfunctioning PLC, due to overheating, which resulted in flaring of acid gas and sour water.

Followup: No

Notes: No information given
114651

2009-05-03
Point Source(s):
Placid's Marine recovery

Pollutant(s):
Volatile Organic Compounds (VOCs) - BRQ
Cause: Placid's Marine vapor recovery unit malfunctioned due to high temperatures.

Followup: No

Notes: no information given. Placid was granted a variance on its title V permit. VOC's controlled by the carbon absorption system to another control device in order to repair the system.
112709

2009-02-11
Point Source(s):
FCCU

Pollutant(s):
FCCU Feed - 0
Cause: Placid's emergency shutdown system was activated in the FCC unit due to a closing control valve and low main air blower discharge flow. During the shutdown valve leaked and the gases ignited. Flaring of debutanizer occurred during start up and shutdown.

Followup: No

Notes: Fire extinguished, eliminated charge from unit, unit brought back online. In addition, training was conducted to prevent similar incidents in the future.
112709

2009-02-11
Point Source(s):
refinery

Pollutant(s):
FCCU Feed - BRQ
Cause: The emergency shutdown system was activated in the FCC unit due to a closing control valve and low main air blower discharge flow. During shutdown, a remote operating valve leaked and the gases ignited. Flaring occurred during start-up and shutdown. Root cause is identified as closed control valve. No information is given on releases.

Followup: No

Notes: Fire was extinguished, eliminated charge from unit, unit brought back online. In addition, training was conducted to prevent similar incidents in the future.