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| LDEQ Incident Number Incident Date |
Point Source/Release | Notes |
| 118307 2009-09-30 | Point Source(s): Sump pump Pollutant(s):Diesel Fuel - BRQ Kerosene - BRQ #6 Oil - BRQ | Cause: A delay in the automatic start-up of sump pump 839 on Placid's south dock allowed oily material to back up into secondary containment. A previously unknown crack in the secondary containment curb allowed material to seep out and cause a sheen. Followup: No Notes: Automatic switches were replaced, and the pump was reset. Also the crack was repaired. |
| 117777 2009-09-06 | Point Source(s): FLARE Pollutant(s):Flammable Gas - BRQ | Cause: planned flaring during start up of an unit. Followup: No Notes: |
| 117362 2009-08-18 | Point Source(s): #2 Sulfur Recover Unit Pollutant(s):Sulfur Dioxide - 1,054 pounds | Cause: Water got into the instrument air system which resulted in the diversion of acid gases to the number three sulfur unit that resulted in the excess emissions from the #2 Sulfur Recover Unit. Followup: No Notes: Police report only. No letter or follow up from the refinery. |
| 116624 2009-07-21 | Point Source(s): FLARE Pollutant(s):Sulfur Dioxide - BRQ | Cause: Water from the farm tank reached the crude unit, that result in flaring of preflash gas. Followup: Yes Notes: No Information Given |
| 116433 2009-07-09 | Point Source(s): Flare Pollutant(s):Sulfur Dioxide - 1,100 pounds | Cause: The released has been happened as a result of flaring during unplanned FCCU shutdown.
On 7/9/09 FCCU experienced an uninterruptible power supply malfunction causing an emergency shutdown valves to go into fail position and flared sour water and wet gas. Followup: No Notes: No information given. The release has be contained within few hours. |
| 116009 2009-06-25 | Point Source(s): Flare Pollutant(s):Sulfur Dioxide - 940 pounds | Cause: Placid#3 sulfur unit experienced a malfunctioning PLC due to overheating. Resulting in the flaring of acid gas and sour water. Followup: No Notes: Placid installed a cooler on the PLC panel. |
| 115997 2009-06-25 | Point Source(s): Flare stack, EQT016, EPN 18-74 Pollutant(s):Sulfur Dioxide - 10,520 pounds | Cause: No. 3 sulfur unit experienced a malfunctioning PLC, due to overheating, which resulted in flaring of acid gas and sour water. Followup: No Notes: No information given |
| 114651 2009-05-03 | Point Source(s): Placid's Marine recovery Pollutant(s):Volatile Organic Compounds (VOCs) - BRQ | Cause: Placid's Marine vapor recovery unit malfunctioned due to high temperatures. Followup: No Notes: no information given. Placid was granted a variance on its title V permit. VOC's controlled by the carbon absorption system to another control device in order to repair the system. |
| 112709 2009-02-11 | Point Source(s): FCCU Pollutant(s):FCCU Feed - 0 | Cause: Placid's emergency shutdown system was activated in the FCC unit due to a closing control valve and low main air blower discharge flow. During the shutdown valve leaked and the gases ignited. Flaring of debutanizer occurred during start up and shutdown. Followup: No Notes: Fire extinguished, eliminated charge from unit, unit brought back online. In addition, training was conducted to prevent similar incidents in the future. |
| 112709 2009-02-11 | Point Source(s): refinery Pollutant(s):FCCU Feed - BRQ | Cause: The emergency shutdown system was activated in the FCC unit due to a closing control valve and low main air blower discharge flow. During shutdown, a remote operating valve leaked and the gases ignited. Flaring occurred during start-up and shutdown. Root cause is identified as closed control valve.
No information is given on releases. Followup: No Notes: Fire was extinguished, eliminated charge from unit, unit brought back online. In addition, training was conducted to prevent similar incidents in the future. |
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